Japan Car

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Citation :on the 13:1 we had stock pistons with head milled 0.080" and block decked 0.040" - doesn't work well - makes very little difference over stock - doesn't seem to breathe right - taking more than 0.040" off the head doesn't improve the performance - 0.040" off head and 0.040" off the block gives you compression ratio of about 11.7:1 with stock pistons - works pretty well, but not a real big hp gain - keeping the head closer to stock with different pistons is a better option

Le mec a rabotté 2mm sur la culasse et 1mm sur le bloc, il obtient un ration 13:1 mais le déconseille. d'aprés lui 1mm sur la culasse suffirait et 0 sur le bloc.

1mm sur la culasse et 1mm sur le bloc, ratio de 11.7:1 marche plutot bien mais pas de gros gain en HP proprement dit.

La meilleure option serait d'après lui de garder la culasse d'origine et changer les pistons.

On parlait de courroie car si on rabote comme lui de belles épaisseurs LOL il faut une courroie un peu plus petite!
1mm avec AAC stock et carto, je trouve ça plutot adapté.
Avec des gros AAC, je raboterais 2mm pour avoir un moteur au comportement qui me convient. Apres chacun ces gouts.
RiB'$ a écrit :
Citation :on the 13:1 we had stock pistons with head milled 0.080" and block decked 0.040" - doesn't work well - makes very little difference over stock - doesn't seem to breathe right - taking more than 0.040" off the head doesn't improve the performance - 0.040" off head and 0.040" off the block gives you compression ratio of about 11.7:1 with stock pistons - works pretty well, but not a real big hp gain - keeping the head closer to stock with different pistons is a better option

Le mec a rabotté 2mm sur la culasse et 1mm sur le bloc, il obtient un ration 13:1 mais le déconseille. d'aprés lui 1mm sur la culasse suffirait et 0 sur le bloc.

1mm sur la culasse et 1mm sur le bloc, ratio de 11.7:1 marche plutot bien mais pas de gros gain en HP proprement dit.

La meilleure option serait d'après lui de garder la culasse d'origine et changer les pistons.

On parlait de courroie car si on rabote comme lui de belles épaisseurs LOL il faut une courroie un peu plus petite!



la sa me va mieu d un coup LOL
je up, j'ai deja posté sur un autre forum, mon niveau en anglais est bon, j'ai à peu pres comprit, mais je dois avouer qu'avoir une traduction precise aiderait.

bon, alors voici un copier coller de ce que j'ai pu trouver sur d-series.org...

que sont ces fameux pistons PM3??

j'ai comprit les grandes lignes et encore, mais est ce que quelqu'un serait capable de traduire ca precisement?

QUOTE The Acid Beaver

The biggest problems with flow are not neccesarily that the ports are too big, it is the whole combustion chamber. It is the worst design from honda, IMO. It is exactly the opposite of what is should be. Ideally a combustion chamber will be compact, have well defined quench areas, enough width for the valves to breath, but maintain a small enough volume to burn quickly and efficiently. The piston should interact with the quench to promote good mixture between air and fuel, prevent detonation, and, again, provide a fast, efficient burn.

The DOHC chamber is frickin huge, so it is not compact. The quench bands are no where near as prominent as they should be. The ports feeding them are very large, which limits velocity and actually hurts flow.

The pistons are really quite horrible, too. They have recessed quench bands, and a HUGE dome that prevents the cumbustion even from spreading quickly and evenly, almost dividing the chamber into three parts. This is just the opposite of what you need!

The biggest reason why ZC heads don't perform even after extensive work, is the pistons that most people use with them. If you use pistons that have higher quench bands (PM3s or PDNs), and are close to flat (PM3s have a slight dish) or a very slight dome (PDNs have a low, wide dome), this wll help the engine run much more optimally. Also, if you take off ~2mm from the head, you bring the existing quench pds down to a level where they can interact with the piston's quench areas and actually do some good for the engine.

I LOVE DOHC Ds, despite thier bad rep. I can't wait to develop some of my theories into working engine setups and test all this out. Not many people put much effort into building these engines NAed, and I don't know if I ever will, but, the engine I am going to build for boost WILL exhibit most of these properties as it will feature zero-decked rollerwaves and ~2mm off the head, which will yeild about 10.5:1 compression for a turbo engine. It will be fine.

Also, don't rev these DOHCs past ~8300RPM. The valve train has been known to fail catastrphically, even with standard mods (springs, retainers, etc) due to the nature of the rockers.

So, my recomendations:

If you want to use PM3 pistons, get some 76mm YCPs from FJT, ARP rod bolts, and have your stock rods shot-peened. Take off ~2mm from the head, or however much you need to get the combustion chambers to ~34.6cc. This, with a .030" headgasket will get you into the 12:1 range. Before wacking the head that much, install cams and head and clay to see how much room you will have. You may need to have the valve reliefs opened up slightly to accomodate the DOHCs larger valves, depending on the cam.

If you want to step it up a notch:
Buy a used set of LS rods. (They go for ~$50 shipped.) Have a machinse shop mod the pistons to fit on a D crank. Get some PDN (98-00 GX) pistons (they are 21mm, just like teh small end of the LS rod), have the SE of the rod trimmed a bit to fit into the piston, and use Y8 rings. Zero-deck the block for the pistons (.5mm off the block), and skim enough of the head to have the combustion chamber at ~38cc (~1mm or so, I need more data to confirm this). This will yeild just shy of 12:1 compression, give you larger valve reliefs, and beefier rods (that aren't retardedly heavy or too expensive).

If you want to use aftermarket pistons, Don't get ones with high domes. The Mid-level ENDYN rollerwaves are good choices. The high domes are not a good combo with this head. (They are more designed to work with the SOHC engines.) Any piston with a compression height of 29.5 or higher (30mm will be at the deck on a stock height block) and a dome of less than 4.5-ish cc will be well suited to the DOHC D.

Happy building!
psyco a écrit :1mm avec AAC stock et carto, je trouve ça plutot adapté.
Avec des gros AAC, je raboterais 2mm pour avoir un moteur au comportement qui me convient. Apres chacun ces gouts.

raboté 2 mm ça risque de ce touché non ?
quel est d'apres vous le gain de puissance obtenu avec rabotage 1mm sur la culasse + AAC stock et PIV évo 2 si la carto convient toujour ...
et du coup quelle épaisseur faut il pour le joint de culasse ?
la carto convient pu Smile
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